Hello everyone. I'm a well seasoned commercial refrig man and I have done my share of auto ACs for friends but I got the crap end of the stick with my owm AC in this dang 2002 Grand Cherokee Ltd! This is the one with the digital AZC and has a hyrdraulic PWM radiator/condenser fan. At test of 100% output at idle it is LOUD and moving lots of air!
When I got it 2 years ago it had already had the compressor, receiver drier, and TXV changed. It worked but this thing is Black, has a sunroof, and is in South MS where it can be 95F with 85%RH or hotter. Well the first thing that happened was the Recirc door and then the blend doors started goofing up. Then the evap developed a leak that summer. So I had the 'pleasure' of pulling the dash and HVAC box out. I put the Heater Treater kits in and while I had everything apart I cleaned and resealed everything better than the factory and put a new heater core, drier, and TXV in there while I was at it and put it all together in a weekend by myself. Yay me!!
Worked good but vent discharge air temps were just not cutting it due to the program cycling the AC clutch off too early it seemed even though it was within factory service manual specs. I added a 1K trimmer resistor across the evap temp sensor (there is NO low pressure switch, only this sensor) and after that I dialed it in as cold as possible without freezing the evap on low fan and low ambient conditions and it has been great!
BUT, there can be better. That hydrofan is barely running even in traffic idle conditions. It does increase and if you rev the engine to 1500 you can see the high side pressure modulate as pretty as the factory specs say. The problem is that those factory specs say 220-300PSI!! And that is at 95F! I see it modulating around 230-250psi at 1300RPM but the fan is turning only a little faster than its idle speed. This fan has plenty of power to go and my traffic idle temps would be a lot better if I could fool that discharge pressure sensor into modulating about 25psi lower than it is.
Here's what I have found so far..... The sensor is a 3 wire transducer that sends 0-5V back to the PCM, The signal is reading 1.27 right now with the AC system On but engine not actually running. Chart says normal range is up to 4.5V and high pressure condition at 4.5-4.8V. So what I think this is telling me is that I need to add my trimmer resistor between the 5v+ and the Signal wire and slowly increase the voltage going back to the PCM to maintain the new pressure I want.
Does that sound right? And if you have done it, what value resistor did you use? I'm planning to use a 1K. I could get a new pressure transducer but I dont think it would be much better than what this one is since its actually running within the factory specs. Of course if I could just reprogram the computer with a new target pressure, none of this would be necessary. LOL! Thanks for reading and any info you have on this system please let me know.
When I got it 2 years ago it had already had the compressor, receiver drier, and TXV changed. It worked but this thing is Black, has a sunroof, and is in South MS where it can be 95F with 85%RH or hotter. Well the first thing that happened was the Recirc door and then the blend doors started goofing up. Then the evap developed a leak that summer. So I had the 'pleasure' of pulling the dash and HVAC box out. I put the Heater Treater kits in and while I had everything apart I cleaned and resealed everything better than the factory and put a new heater core, drier, and TXV in there while I was at it and put it all together in a weekend by myself. Yay me!!
Worked good but vent discharge air temps were just not cutting it due to the program cycling the AC clutch off too early it seemed even though it was within factory service manual specs. I added a 1K trimmer resistor across the evap temp sensor (there is NO low pressure switch, only this sensor) and after that I dialed it in as cold as possible without freezing the evap on low fan and low ambient conditions and it has been great!
BUT, there can be better. That hydrofan is barely running even in traffic idle conditions. It does increase and if you rev the engine to 1500 you can see the high side pressure modulate as pretty as the factory specs say. The problem is that those factory specs say 220-300PSI!! And that is at 95F! I see it modulating around 230-250psi at 1300RPM but the fan is turning only a little faster than its idle speed. This fan has plenty of power to go and my traffic idle temps would be a lot better if I could fool that discharge pressure sensor into modulating about 25psi lower than it is.
Here's what I have found so far..... The sensor is a 3 wire transducer that sends 0-5V back to the PCM, The signal is reading 1.27 right now with the AC system On but engine not actually running. Chart says normal range is up to 4.5V and high pressure condition at 4.5-4.8V. So what I think this is telling me is that I need to add my trimmer resistor between the 5v+ and the Signal wire and slowly increase the voltage going back to the PCM to maintain the new pressure I want.
Does that sound right? And if you have done it, what value resistor did you use? I'm planning to use a 1K. I could get a new pressure transducer but I dont think it would be much better than what this one is since its actually running within the factory specs. Of course if I could just reprogram the computer with a new target pressure, none of this would be necessary. LOL! Thanks for reading and any info you have on this system please let me know.
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